Welcome to the Australian Ford Forums forum.

You are currently viewing our boards as a guest which gives you limited access to view most discussions and inserts advertising. By joining our free community you will have access to post topics, communicate privately with other members, respond to polls, upload content and access many other special features without post based advertising banners. Registration is simple and absolutely free so please, join our community today!

If you have any problems with the registration process or your account login, please contact us.

Please Note: All new registrations go through a manual approval queue to keep spammers out. This is checked twice each day so there will be a delay before your registration is activated.

Go Back   Australian Ford Forums > Club and Speciality Forums > Forum Community Car Clubs > AU Falcon.com.au

Reply
 
Thread Tools Display Modes
Old 28-02-2009, 02:18 PM   #1
honer
Back to N/A land
 
Join Date: Jan 2005
Location: Perth
Posts: 610
Default Any ideas ?

Dudes

Got a weird issue that I really can't figure out why is occuring

Basically, when the car revs (usually 1/2 to full throttle) when it hits about 3000rpm it basically feels like it "pulls back" (kind of like traction control feel) and feels doughy up top, almost like its pulling out alot of timing something.

This was happening last week (as well as a massive miss) however I put new leads, plugs and air filter in which has fixed all the missing, however this issue still remains (though not AS noticable)

Any ideas ?

BTW car is AU3 XR8..

honer is offline   Reply With Quote Multi-Quote with this Post
Old 28-02-2009, 04:14 PM   #2
Bushbasher
When in doubt, GAS IT!!
 
Bushbasher's Avatar
 
Join Date: Sep 2006
Location: Lower Eyre Peninsula, SA
Posts: 3,018
Default

It's not leaning out is it? put a bottle of injector cleaner through it and change your fuel filter and see if that makes a difference.

Bushbasher
__________________
.





HERS- BFIII Wagon Gold, alloys, dual fuel, bullbar, big tow pack, trans cooler, fully rebuilt HD suspension, Clarion, alarmed, full 2 1/2" sports system, mint body

MINE- AUII Forte
Meteorite, dual fuel but otherwise bog stock.

MINE- AUII Fairlane Sportsman Liquid Silver over meteorite,HIDs', Airhog, Eagle Leads, dual fuel, custom rear springs, BA slotted discs + a second one for spares

.
Bushbasher is offline   Reply With Quote Multi-Quote with this Post
Old 28-02-2009, 04:28 PM   #3
LG
FF.Com.Au Hardcore
 
LG's Avatar
 
Join Date: Dec 2004
Location: Melbourne, Victoria
Posts: 2,434
Default

Is this with < 1/4 of fuel?
__________________
AUIII Falcon Forte, with SIX Appeal
LG is offline   Reply With Quote Multi-Quote with this Post
Old 28-02-2009, 04:32 PM   #4
Peuty
Afterburner + skids =
Donating Member1
 
Peuty's Avatar
 
Join Date: Dec 2004
Location: Skidsville
Posts: 12,146
Default

Could be a breakdown in the coils as well. Are they the original coils?

Also, can you hear any pinging?
__________________
Speed Kills. So buy an AU XR8 and live forever.

Oo\===/oO
Peuty is offline   Reply With Quote Multi-Quote with this Post
Old 28-02-2009, 05:37 PM   #5
TURBOTAXI
Turbo Falcon Fiend
 
TURBOTAXI's Avatar
 
Join Date: May 2005
Location: Far West NSW
Posts: 3,213
Default

Quote:
Originally Posted by Peuty
Could be a breakdown in the coils as well. Are they the original coils?

Also, can you hear any pinging?

Thats what I was thinking
__________________
Just a few.
TURBOTAXI is offline   Reply With Quote Multi-Quote with this Post
Old 28-02-2009, 05:42 PM   #6
JC
Miami Pilot
Donating Member2
 
JC's Avatar
 
Join Date: Jan 2005
Location: ACT
Posts: 21,704
Tech Writer: Recognition for the technical writers of AFF - Issue reason: Writing tech articles 
Default

Could also be a blocked cat
__________________
-----------------------------------------------------------------
The Hammer: FG GTE | 376rwkw | 1/4 mile 11.793 @ 119.75mph 1.733 60' (4408lb)
1 of 60 FG MK1 335 GTEs (1 of 118 FG Mk 1 & 2 335 GTEs).
Mods: Tune, HSD/ShockWorks, black GT335 19” staggered replicas with 245 & 275/35/19 Michelin Pilot sport 5s

Daily: BF2 Fairmont Ghia I6 ZF, machine face GT335 19” staggered Replicas with 245s and 275s, Bilsteins & Kings

FPV 335 build stats: <click here>

Ford Performance Club ACT
JC is offline   Reply With Quote Multi-Quote with this Post
Old 02-03-2009, 10:39 AM   #7
autickfordfairmont
Tickford Equiped
 
autickfordfairmont's Avatar
 
Join Date: Jan 2005
Location: Tweed Coast
Posts: 418
Default

Another vote for a blocked cat.

I had a similar thing with mine where first it was the fuel pump oversuppling fuel (looked like a diesel truck when driving), after that was fixed, about 2 months later i had your symptoms. I took it to my mechanic and they spent 2 days on it, got specialist equipment down from brisbane and all sorts, in the end it turned out to be a collapsed cat (obviously from the overfuelling issue). New high flow cat & a tune up & the thing went better and harder than it ever had before. A new cat (or two in your case) isnt cheap, so try replacing the fuel filter, clean the filter sock on the pump & run some injector cleaner through it to see if that clears it all up first.
If that doesnt then check the cats.
Also, try disconnecting the battery and letting the computer reset overnight. It may sound simple, but it has fixed many a problem with my car that I thought would have been something else.
Cheers

Col.
__________________
Genuine Tickford Equiped 1998 AU Fairmont
Mods: ....... Dash mat & Air Freshener, does that count as a mod??????
Sports Exahust, Tickford Intake Snorkle, K&N Filter, NGK Plugs, Top Gun Leads
TS50 Front Bar with Fog lights, TS50 Rear Bar. Injected LPG System,
autickfordfairmont is offline   Reply With Quote Multi-Quote with this Post
Old 02-03-2009, 07:14 PM   #8
Peuty
Afterburner + skids =
Donating Member1
 
Peuty's Avatar
 
Join Date: Dec 2004
Location: Skidsville
Posts: 12,146
Default

Quote:
Originally Posted by autickfordfairmont
I took it to my mechanic and they spent 2 days on it, got specialist equipment down from brisbane and all sorts, in the end it turned out to be a collapsed cat
Time to find a new mechanic if he needed specialist equipment to diagnose a busted cat.
__________________
Speed Kills. So buy an AU XR8 and live forever.

Oo\===/oO
Peuty is offline   Reply With Quote Multi-Quote with this Post
Old 02-03-2009, 08:35 PM   #9
adrian k
adrian
 
adrian k's Avatar
 
Join Date: Aug 2005
Location: Christchurch, New Zealand
Posts: 495
Default

na, my XR8 did just that and i don't have any cats. Ford cleaned the TB and reset the ECU and i put a bottle of injector cleaner thru it, and the flat spotting is all but gone now, really have to pay close attention to notice only the slightest hesitation.
months before i had already had the fuel pump changed out due to the 1/4 tank surging issue.
__________________
T3 TS50 #17 275kW
AU3 XR8 SVP 220kW
adrian k is offline   Reply With Quote Multi-Quote with this Post
Old 03-03-2009, 09:56 AM   #10
autickfordfairmont
Tickford Equiped
 
autickfordfairmont's Avatar
 
Join Date: Jan 2005
Location: Tweed Coast
Posts: 418
Default

Quote:
Originally Posted by Peuty
Time to find a new mechanic if he needed specialist equipment to diagnose a busted cat.
The way it was behaving seemed like a collapsed cat, but when they dropped off the pipe and had a look it all looked ok, was only after they tried everything else first that we chucked the new cat on and it fixed it. All up they spent 14 hours in total on it trying & testing different things, and I only got charged for 1 hour labour. Whatever they did to it over the two days, and the tune up they did was bloody awsome. After the new cat it was the quickest it had ever been. And for a fairly bog stock standard Fairmont (apart from exhaust and intake) it would blow the absolute hell out of my brothers EL XR6 & also his new WRX.
__________________
Genuine Tickford Equiped 1998 AU Fairmont
Mods: ....... Dash mat & Air Freshener, does that count as a mod??????
Sports Exahust, Tickford Intake Snorkle, K&N Filter, NGK Plugs, Top Gun Leads
TS50 Front Bar with Fog lights, TS50 Rear Bar. Injected LPG System,
autickfordfairmont is offline   Reply With Quote Multi-Quote with this Post
Old 03-03-2009, 01:06 PM   #11
honer
Back to N/A land
 
Join Date: Jan 2005
Location: Perth
Posts: 610
Default

Cheers dudes

Fuel filter is new, the issue was occuring under 1/4 tank, however I'm sure it was occuring above that level as well.. But I'll check it again to make sure (My EL XR8 suffered the 1/4 tank issue as well)

I'll see if I can borrow some coils as well and see if that helps out...

If it ends up looking like the cats and I'll just have to buy a couple cats and some bends and build a new exhaust rather then just replacing the cats (Exhaust system has def seen better days)
honer is offline   Reply With Quote Multi-Quote with this Post
Reply


Forum Jump


All times are GMT +11. The time now is 01:08 AM.


Powered by vBulletin® Version 3.8.5
Copyright ©2000 - 2024, Jelsoft Enterprises Ltd.
Other than what is legally copyrighted by the respective owners, this site is copyright www.fordforums.com.au
Positive SSL